Fix compile error with JUNCTION_DEVIATION

See #13000
This commit is contained in:
Scott Lahteine 2019-02-20 04:54:17 -06:00
parent 758c6c9464
commit 3c9a7926c2

View file

@ -2036,6 +2036,15 @@ void MarlinSettings::reset(PORTARG_SOLO) {
planner.settings.min_travel_feedrate_mm_s = DEFAULT_MINTRAVELFEEDRATE; planner.settings.min_travel_feedrate_mm_s = DEFAULT_MINTRAVELFEEDRATE;
#if HAS_CLASSIC_JERK #if HAS_CLASSIC_JERK
#ifndef DEFAULT_XJERK
#define DEFAULT_XJERK 0
#endif
#ifndef DEFAULT_YJERK
#define DEFAULT_YJERK 0
#endif
#ifndef DEFAULT_ZJERK
#define DEFAULT_ZJERK 0
#endif
planner.max_jerk[X_AXIS] = DEFAULT_XJERK; planner.max_jerk[X_AXIS] = DEFAULT_XJERK;
planner.max_jerk[Y_AXIS] = DEFAULT_YJERK; planner.max_jerk[Y_AXIS] = DEFAULT_YJERK;
planner.max_jerk[Z_AXIS] = DEFAULT_ZJERK; planner.max_jerk[Z_AXIS] = DEFAULT_ZJERK;